I setup everything an tested. At the end, I didn't like the final result. The movement is very jerky and Cetus remote interface leads to latency increase and sudden stops. It just can't work together on Beaglebone. With local interface, like tklinuxcnc it works, but my goal is working without LCD. I move to Arduino mega.
Discussions
Become a Hackaday.io Member
Create an account to leave a comment. Already have an account? Log In.