Inverted pendulum system using 12V 775 DC motor, driven by L298N motor driver.
Controlled by a joystick interfaced using an arduino uno.
observations:
- Irregular and abrupt motions.
- Motor unable to provide enough torque
- difficulty in precise controlling of the motor
inferences:
- Driver limitations 2A output per channel. Hence, could not provide enough torque for smooth transmission.
- Mechanism is smooth without the motor involved.
Discussions
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