As i mentioned in previous log entry I tried to mount the magnetometer close to the anemoscope. This idea turned out to be wrong as the anemoscope has a megnt built-in.
I moved the magnetometer further by designing and printing 15 centimeter long offsetting element.
After calibration the compass works fine :)
I'd also like to mention that current software (embedded and PC app) is available at GitHub.
Embedded code: https://github.com/Lukaszm94/rocketLauncherDAQ_embedded
PC application: https://github.com/Lukaszm94/RocketLauncherDataAcquisitionApp
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