Lot of work finished, and also lot ahead.
The driver and the measurement is working:
And here is the current state of the schematics:
I'll explain the operation in a later post. Now just the things still ahead:
- A few mV noise is still on the motor's rail, what I want to filter out. In addition I want to change the current passive measurement filter to a 2nd order active Chebyshev filter.
- The complete PWM generator, frequency measurement, display, PID controller is ahead.
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